I decided to take a break from being scrunched up working under the cockpit and started working on the head so I could work more comfortably for a while. I sat across from the head and visualized the components and where they might go. I cut some plywood, made a mock-up, and placed the toilet on the plinth and stared at it until I had a good picture in my mind of what I wanted to build.
While waiting for panels to be ready I started preparing the head area. The fiberglass was sanded and cleaned. The listings for the panels were installed and the mounting pads for the strainer, pump, and vented loop were fabricated and epoxied into place and filleted. The space behind the panels was painted with Pettit Dura White paint, Pettit claims mould and mildew will not grow on this paint. I have not been able to get the paint to flow and level well regardless of the technique used to apply it. Several types of rollers were tried as well as rolling and tipping, and applying with good quality badger brushes. The finish is suitable for lockers but I will have to experiment with it further to see if I can get better results for use in the cabin.
Several layers of biaxial cloth was applied to seal the 1-1/2" hole in the hull where the old toilet discharged directly overboard. A location was chosen for the intake thru-hull and several layers of biaxial cloth was applied to the hull starting with a large piece and gradually reducing each subsequent piece in size. The next day the adapter flange was test fit and epoxy with high density filler was used to level the area under the flange. This method makes for a very strong, thick base for the thru-hull assembly and a traditional wood backing plate is not required. The problems of compression fatigue and breakdown or rot of a traditional wood backing block is eliminated.
Contact adhesive was sprayed onto the hull and onto the Double-bubble insulation that was previously cut to a slightly larger size than required. The insulation was then pressed into place and a razor knife was used to trim the edges. Shrink wrap tape was used to join seams. A heat gun was used to warm the tape and ensure it would not separate with age. If you don't use heat on the tape it often will lift with age. If you use heat it is extremely difficult to remove and will not lift with age.

